I have a M98-8K PLUS Magcubic TV-Box based on the Allwinner H618 SOC.
On board is a Sp6330 wifi/bt module that requires a 32kHz clock to
operate correctly. Without this change the clock from the SOC is
~29kHz and BT module does not start up. The patch enables the Internal
OSC Clock Auto Calibration of the H616/H618 which than provides the
necessary 32kHz and the BT module initializes successfully.
Add a flag and set it for H6.
Also the code is developed on the H618 board it only modifies the H6 as
there is no support for H616/H618 in the current code.
Signed-off-by: Alois Fertl <[email protected]>
---
v1->v2
- add flag and activate for H6 AND H616
v2->v3
- correct findings from review
v3->v4
- adjust to mainline tree
I have also tried to test this using the new driver in sunxi-ng
manually injecting the reverted patch
https://git.kernel.org/pub/scm/linux/kernel/git/torvalds/linux.git/commit/?id=60d9f050da63b
The code in drivers/clk/sunxi-ng/ccu-sun6i-rtc.c is being called and it
initializes the relevant registers to the same values as the old driver,
but the change ends up with a system that often hangs during booting and
only ocasionally reaches the login state (one out of 10).
The main difference I see adhoc is that the old drivers init is done
using CLK_OF_DECLARE_DRIVER so initialization is done very early.
The new driver does the initialisation via probe which is quite some
time later.
Can't tell if this is the cause for the problems.
---
drivers/rtc/rtc-sun6i.c | 16 +++++++++++++++-
1 file changed, 15 insertions(+), 1 deletion(-)
diff --git a/drivers/rtc/rtc-sun6i.c b/drivers/rtc/rtc-sun6i.c
index 8e0c66906..57aa52d3b 100644
--- a/drivers/rtc/rtc-sun6i.c
+++ b/drivers/rtc/rtc-sun6i.c
@@ -42,6 +42,11 @@
#define SUN6I_LOSC_CLK_PRESCAL 0x0008
+#define SUN6I_LOSC_CLK_AUTO_CAL 0x000c
+#define SUN6I_LOSC_CLK_AUTO_CAL_16MS BIT(2)
+#define SUN6I_LOSC_CLK_AUTO_CAL_ENABLE BIT(1)
+#define SUN6I_LOSC_CLK_AUTO_CAL_SEL_CAL BIT(0)
+
/* RTC */
#define SUN6I_RTC_YMD 0x0010
#define SUN6I_RTC_HMS 0x0014
@@ -126,7 +131,6 @@
* registers (R40, H6)
* - SYS power domain controls (R40)
* - DCXO controls (H6)
- * - RC oscillator calibration (H6)
*
* These functions are not covered by this driver.
*/
@@ -137,6 +141,7 @@ struct sun6i_rtc_clk_data {
unsigned int has_out_clk : 1;
unsigned int has_losc_en : 1;
unsigned int has_auto_swt : 1;
+ unsigned int has_auto_cal : 1;
};
#define RTC_LINEAR_DAY BIT(0)
@@ -267,6 +272,14 @@ static void __init sun6i_rtc_clk_init(struct device_node *node,
}
writel(reg, rtc->base + SUN6I_LOSC_CTRL);
+ if (rtc->data->has_auto_cal) {
+ /* Enable internal OSC clock auto calibration */
+ reg = SUN6I_LOSC_CLK_AUTO_CAL_16MS |
+ SUN6I_LOSC_CLK_AUTO_CAL_ENABLE |
+ SUN6I_LOSC_CLK_AUTO_CAL_SEL_CAL;
+ writel(reg, rtc->base + SUN6I_LOSC_CLK_AUTO_CAL);
+ }
+
/* Yes, I know, this is ugly. */
sun6i_rtc = rtc;
@@ -374,6 +387,7 @@ static const struct sun6i_rtc_clk_data sun50i_h6_rtc_data = {
.has_out_clk = 1,
.has_losc_en = 1,
.has_auto_swt = 1,
+ .has_auto_cal = 1,
};
static void __init sun50i_h6_rtc_clk_init(struct device_node *node)
--
2.39.2
On Wed, 22 May 2024 20:28:26 +0200
Alois Fertl <[email protected]> wrote:
> I have a M98-8K PLUS Magcubic TV-Box based on the Allwinner H618 SOC.
> On board is a Sp6330 wifi/bt module that requires a 32kHz clock to
> operate correctly. Without this change the clock from the SOC is
> ~29kHz and BT module does not start up. The patch enables the Internal
> OSC Clock Auto Calibration of the H616/H618 which than provides the
> necessary 32kHz and the BT module initializes successfully.
> Add a flag and set it for H6.
> Also the code is developed on the H618 board it only modifies the H6 as
> there is no support for H616/H618 in the current code.
I am a bit confused: so this patch doesn't fix your problem then, because
the code you touch is not used on the H616/H618?
Actually I would have expected your patch to only change
drivers/clk/sunxi-ng/ccu-sun6i-rtc.c, since that's the only RTC clock
driver relevant for the H616.
> Signed-off-by: Alois Fertl <[email protected]>
> ---
>
> v1->v2
> - add flag and activate for H6 AND H616
>
> v2->v3
> - correct findings from review
>
> v3->v4
> - adjust to mainline tree
>
> I have also tried to test this using the new driver in sunxi-ng
> manually injecting the reverted patch
> https://git.kernel.org/pub/scm/linux/kernel/git/torvalds/linux.git/commit/?id=60d9f050da63b
So this was done on a H6 device? Because out of the box rtc-sun6i.c is
used on the H6 only, and ccu-sun6i-rtc.c is only used on the H616.
Maybe I am missing something here ...
> The code in drivers/clk/sunxi-ng/ccu-sun6i-rtc.c is being called and it
> initializes the relevant registers to the same values as the old driver,
> but the change ends up with a system that often hangs during booting and
> only ocasionally reaches the login state (one out of 10).
> The main difference I see adhoc is that the old drivers init is done
> using CLK_OF_DECLARE_DRIVER so initialization is done very early.
> The new driver does the initialisation via probe which is quite some
> time later.
> Can't tell if this is the cause for the problems.
That sounds odd, can you post your changes somewhere?
Generally, without a proper problem and without further testing, I would
not like to touch the H6 RTC code needlessly.
For the H616 we have a concrete problem at hand, that justifies a change,
also it's the proper driver for new devices, so that's where the change
should happen.
Cheers,
Andre
>
> ---
> drivers/rtc/rtc-sun6i.c | 16 +++++++++++++++-
> 1 file changed, 15 insertions(+), 1 deletion(-)
>
> diff --git a/drivers/rtc/rtc-sun6i.c b/drivers/rtc/rtc-sun6i.c
> index 8e0c66906..57aa52d3b 100644
> --- a/drivers/rtc/rtc-sun6i.c
> +++ b/drivers/rtc/rtc-sun6i.c
> @@ -42,6 +42,11 @@
>
> #define SUN6I_LOSC_CLK_PRESCAL 0x0008
>
> +#define SUN6I_LOSC_CLK_AUTO_CAL 0x000c
> +#define SUN6I_LOSC_CLK_AUTO_CAL_16MS BIT(2)
> +#define SUN6I_LOSC_CLK_AUTO_CAL_ENABLE BIT(1)
> +#define SUN6I_LOSC_CLK_AUTO_CAL_SEL_CAL BIT(0)
> +
> /* RTC */
> #define SUN6I_RTC_YMD 0x0010
> #define SUN6I_RTC_HMS 0x0014
> @@ -126,7 +131,6 @@
> * registers (R40, H6)
> * - SYS power domain controls (R40)
> * - DCXO controls (H6)
> - * - RC oscillator calibration (H6)
> *
> * These functions are not covered by this driver.
> */
> @@ -137,6 +141,7 @@ struct sun6i_rtc_clk_data {
> unsigned int has_out_clk : 1;
> unsigned int has_losc_en : 1;
> unsigned int has_auto_swt : 1;
> + unsigned int has_auto_cal : 1;
> };
>
> #define RTC_LINEAR_DAY BIT(0)
> @@ -267,6 +272,14 @@ static void __init sun6i_rtc_clk_init(struct device_node *node,
> }
> writel(reg, rtc->base + SUN6I_LOSC_CTRL);
>
> + if (rtc->data->has_auto_cal) {
> + /* Enable internal OSC clock auto calibration */
> + reg = SUN6I_LOSC_CLK_AUTO_CAL_16MS |
> + SUN6I_LOSC_CLK_AUTO_CAL_ENABLE |
> + SUN6I_LOSC_CLK_AUTO_CAL_SEL_CAL;
> + writel(reg, rtc->base + SUN6I_LOSC_CLK_AUTO_CAL);
> + }
> +
> /* Yes, I know, this is ugly. */
> sun6i_rtc = rtc;
>
> @@ -374,6 +387,7 @@ static const struct sun6i_rtc_clk_data sun50i_h6_rtc_data = {
> .has_out_clk = 1,
> .has_losc_en = 1,
> .has_auto_swt = 1,
> + .has_auto_cal = 1,
> };
>
> static void __init sun50i_h6_rtc_clk_init(struct device_node *node)